ICOM 746 and 746Pro

 LCD Back Light and Dead Transmitter Repair

Dave Sparks, KV5A



[email protected]

The ICOM 746Pro has two well known problems. The LCD display back light driver transistor will eventually dissipate way too much heat and fail. In the  worst case, the result is a carbonized PC board and lifted mounting pads. Your display goes dark. You can live without it but the display is almost impossible to see in a low light environment. The other issue is the sudden death of your transmitter.  That means your backup transceiver will have to take up the slack while your 746 rig is off the the repair facility. Doing the repair yourself will save you a bunch of time and money but do this only if you can work with small SMD components and have the proper tools to do so. There are several solutions published on line by hams who have had these failures.  You can decide if their solutions meet your requirements. Mark, K5LXP, has a very informative article at the link below.
Mark provides details for this repair I will not duplicate here.
http://www.qsl.net/k5lxp/projects/746Pro/746ProNoTX.html

 Ed, WA3WJS provides this intuitive article at this link below.
https://wa3wsj.homestead.com/IC-746Pro_Sudeden__Death_Fixes.pdf


The following is my analysis and the repair I decided to do. I do not guarantee your results if you attempt to duplicate my repairs but I think you will find it is a thoughtful approach.  

The 746/Pro Sudden Transmitter Death 

My research of all the posts I read indicates there may be several possible causes of the failure of RF transmit driver IC-151, uPC1678G. Among them are ESD, excessive heat dissipation, and a high voltage spike on the 5 volt supply line.  All of these possibilities are plausible. The failures seem to occur over various periods of time and under different circumstances making it difficult to pin down the exact cause. Ed, WA3WSJ, posted an article on this issue.  I was convinced he was on to something. In short, he had a friend whose coworker had a problem with a similar circuit design. He kept blowing a like RF IC chip trying to get it to work, but why? The reason discovered was that the manufacturer's design called for a nanoHenry choke in the 5V supply line and not a uHenry choke. Thus, every time the power supply was turned on the chip's collector output was hit with a large inductive spike eventually blowing it out. Replacing the choke with a smaller choke did the trick and the circuit worked just fine. If heat dissipation is not the issue then adding a heat sink is not necessary.  So, with that in mind,  instead of duplicating other repairs, I approached the repair as follows.
 
⦁    1. Replace IC-151 with a new uPC1678G available from Circuitstransistors.com. $4.00 each plus shipping as of May 1, 2018.
⦁    2. Replace C156 .0047 uf chip cap with a 20uf chip cap. (or two 10 uf caps,  DigiKey part number 445-11219-1-ND) This will filter the Vcc chip supply and eliminate any excessive inductive spike to the chip output collector. This is likely the only modification really necessary.
⦁    3. Lift R157 10 ohm resistor from the +5.0 volt supply, stand it on end attached to the pad nearest IC pin 8. Connect the anode end of a 2.7 volt zener (DigiKey part number 1N5223BCT-ND) to the lifted end of R157 and solder the cathode end to the transmit 8 volt line at R156 330 ohm resistor. This will supply power to the chip only on transmit. This might not be necessary but it does no harm.
 ⦁    4. Add a 1 mH choke (DigiKey part number RLB0608-102K-ND)  to the center pin of the HRX connector (J1) and the PCB ground plane. This is for added ESD protection. K5LXP suggests this and it too does no harm. Time will tell if my solution will hold up. So far so good.

 
ICOM 746Pro RF Unit PC Board
Figure 1.
This is the ICOM 746Pro RF Unit PC Board where the driver chip circuit is found. IC-151 is located on the left side.


Close up of the new uPC1678G chip
Figure 2.
Close up of the new uPC1678G chip installed and two 10 uF caps stacked to replace C-156. Also shown is a 2.7 volt zener attached to the 8 volt transmit supply line.


1 mH choke is installed
Figure 3.
A 1 mH choke is installed on the bottom of the board for added ESD protection. The pin diodes were factory installed and were not changed.


CR-338 High Stability Crystal Unit
Figure 4.
While I had the radio opened up, I added the optional the CR-338 High Stability Crystal Unit to the same board. This provides better frequency stability and accuracy especially noticeable on 6 and 2 meters.

746 LCD Back Light

The LCD back light issue eventually plagues every 746Pro. I bought my rig at a tailgate a few years ago and it was not long till the intermittent back light on again and off again symptom appeared. Eventually it stopped working all together and I lived with it for a long time. Now is the time to get my back light back. The common cause of this failure is excessive heat dissipation in the high voltage driver transistor, especially when the brightness is set to less than 100%. The transistor dissipates more power at lower brightness settings contributing to the failure. The root cause is of course a very poor ICOM design.
 
KA1MDA has a very informative and detailed article here:
http://www.ka1mda.org/ham/homebrew/746/index.htm

 Several of the repairs I found on the WEB included adding a heat sink inside the shield cage and that is ok, but the heat sink was not attached to the tab of Q302 in any of these repairs. It was maybe touching the plastic case because of the mechanical implementation. This was not very effective in my opinion. The transistor tab is where the heat sink needs to be attached to effectively cool the transistor junction.  So, I decided to take a different approach.
I ordered more than one of each part replaced just in case, well just in case... and then thought about what I needed to do. Parts are available from DigiKey. Direct replacements are Q302, 2SB1201-TL-E, C-303, EEE-1CA470SP, Cap Alum 10uf, 20% 16V SMD, and C302, EEE-1CA100SR, Cap Alum 10uf 20% 16V SMD.  All the other parts came from my junk box. The copper plate is .0675" thick cut to fit inside the shield less about 1/16"all around so as to not touch the PCB or the shield. The fiber shoulder washer fits into a 1/4" hole in the shield. The mounting screw is 4-40 cut to length to fit the thickness of the shield, cooper plate and the little IC heat sink plus a few threads for the nut. The silicone insulator is a strip cut to size from a silicone rubber oven glove available from many grocery or kitchen supply stores. The material used is .052 " thick.  You might even have one at home already. The thermal compound and all the tools or other material to fabricate my heat sink assembly were on hand.


Back of the front panel
Figure 5.
This is the back of the front panel as removed from the body of the 746Pro. The ribbon cables and connectors must be disconnected and the the mounting screws are removed in order to carefully separate this board from the remaining front panel circuitry. There are two pot mounting nuts that also must be removed.

Here is a video detailing the disassembly of the front panel.
https://www.youtube.com/watch?v=3JWFYIl3zTc


Defective Q302, 2SB1201
Figure 6.
The defective Q302, 2SB1201, is shown here in the bottom right of the shield. The PC board shows discoloration due to excessive heat.


PCB is burned
Figure 7.
The transistor and associated capacitors were removed. The pads where Q302 was soldered lifted from the PCB. The PCB is burned and the surrounding area is discolored.  I scraped as much of the carbon off the board as possible. The shield around the components was removed to effect the repair.


Q302 soldered to new heat sink
Figure 8.
Since there is no way to secure the transistor to the PCB as in the original design, I chose to mount the transistor vertically and attach a heat sink directly to the transistor tab. The copper sheet shown here is slightly more
thick than a penny. Notice the cut out for clearance of C-302, 10uf cap. Both (C-303) 47uf, and (C-302) 10uf, capacitors are replaced in case they were damaged.

Fiber shoulder washer
Figure 9.
The heat sink must be insulated from the shield since the collector is at a high voltage potential.  I used a small strip of material from a green colored silicon oven glove. It is a good heat and electrical insulator.  I added a small IC heat sink for added radiation of the heat. The assembly is mounded to the inside of the cage with a 4-40 screw and a fiber shoulder washer on the outside of the cage. Thermal grease is applied between the copper and the black heat sink.


New heat sink and insulator
Figure 10.
Q302 is solidly soldered to the copper sheet. A small amount of the black heat sink is filed away to clear a nearby transistor. The legs of transistor Q302 are bent up to enable adding #30 wire wrap wire to make the connections to the PCB.


Shield mounted on PCB
Figure 11.
The heat sink assembly is mounted to the shield, and Q302 connections are soldered to the proper points on the PCB with #30 wire wrap wire.  Red nail polish is painted on the board to cover an area of exposed ground plane and to provide mechanical stability for a loose trace on the PCB. A small piece of the silicone material is between the PCB and Q302 legs to insulate it from the near by ground plane.


Vent holes drilled in shield lid
Figure 12.
I drilled several holes in the shield lid just above the black heat sink to facilitate the escape of radiated heat. An additional piece of the silicone insulator was glued inside the lid just above Q302 as mounted to prevent the copper sheet from possible contact with the lid. The mounting screw is tightened enough to prevent rotation of the heat sink assembly within the shield.  I applied locktite to the 4-40 screw threads during assembly. With the silicone in place at the top and bottom of Q302 the heat sink will stay in place.


Screw head close to encoder body
Figure 13.
The PCB is now re-attached to the front panel assembly. The mounting screw head on the shield is very close to the encoder body though it is not touching. For added protection, I put a piece of electrical tape on the encoder body just in case anything moves. If you look carefully you can see the black shoulder washer on the outside of the shield.
The head of the screw could be filed down for greater clearance but I did not think it was necessary, but that depends on the particular hardware used in any case.

A bright 746 display
Figure 15.
After a careful re-assembly of the front panel and installing the top and bottom cover back on the radio, I'm ready for the the smoke test. Holy Cow! The display is fixed and the transmitter is back to full output power. The transmitter is working like new too.  Happy days are here again!

Parts are available from DigiKey for the Back Light repair. Direct replacements are Q302, 2SB1201-TL-E, C-303, EEE-1CA470SP, Cap Alum 10uf, 20% 16V SMD, and C302, EEE-1CA100SR, Cap Alum 10uf 20% 16V SMD.  All the other parts came from my junk box. The copper plate is .0675" thick cut to fit inside the shield less about 1/16"or more all around so as to not touch the PCB or the shield. The fiber shoulder washer fits into a 1/4" hole in the shield. The mounting screw is size 4-40 cut to length to fit the total thickness of the shield, cooper plate, silicone insulator, and the little IC heat sink plus a few threads for the nut. The silicone insulator is a strip cut to size from a silicone rubber oven glove available from a grocery or kitchen supply store. The material I used is .062" thick. The thermal compound, other supplies and all the tools to perform this repair were on hand. Thanks to  K5LXP, WA3WSJ, KA1MDA and many others for their contribution to the understanding of these problems and their take on subsequent repairs.
Now on to the next project.
If you have comments or questions please email. 
73, KV5A, Dave

[email protected]