PROBLEM: Distortion level in SSB transmitted signal not acceptable. FIXES: 1. Increase the supply V to the max rated16VDC to give the collectors more headroom, 2. See service manual. Increase the bias (VR1) in the driver from 200mA (service manual) to 250mA. Increase the bias (VR2) in the final from 200mA (service manual) to 400mA // note - the bias adjustments are accessed through two holes in the back of the heatsink. The hole nearest the Antenna jack is VR1. The access hole farther away from the Antenna jack is VR2.
PROBLEM: Limited transmit frequency coverage. FIX: Cut D80 on the Control Unit for 1.6MHz to 30MHz transmit capability. D80 is about 2" from D66, which is cut for 10Hz frequency readout.
PROBLEM: Lack of crispness in the RX audio, which makes the sibilant
parts of human speech hard to distinguish from each other. This is
caused by a 5db roll-off at 3000Hz in the RX audio. FIX: Change C51
[0.033µF] on the IF Unit, near L5, to .005µF [5000pF/5nF].
This will reduce the roll-off to a more acceptable 1.4db at 3000Hz.
"After modification, the RF Gain control should be backed off [CCW]
until the band/sky-noise decreases to a comfortable listening level.
This will not interfere with the reception of moderately weak
signals.
PROBLEM: Even while listening on a large, external speaker, music
sounds flat and tinny because the audio frequency response rolls off
below 200Hz. FIX: There are a number of capacitors in the RX audio
amplifier circuits that can be increased in capacitance to restore
the low-end audio. These capacitors are in the IF Unit. They are:
C60, C66. C67, C69, C170 and C175. The increase in capacitance should
be 4 times. {Note: Some capacitors in the audio circuitry can not be
arbitrarily increased in value without causing unacceptable
tradeoffs.} C175 can be replaced with a 1000µF, 10V unit, whose
full-length leads are sheathed in Teflon sleeving, except for the
last 8mm, to allow soldering to the PC board. This is done because
the board-space allotment for the stock C175 is too small for the
larger, replacement unit. The new capacitor is folded over and tucked
in appropriately.
PROBLEM: Tinny/thin-sounding transmit audio. FIX: On the IF Unit,
change C135 {0.1µF}, near the center-board fastening screw, to
0.47µF.
PROBLEM: The stock, muRata CFJ455K14 SSB filter in the 455KHz IF
has a selectivity shape-factor of 2 to 1. This is definitely less
than wonderful. The stock SSB filter in the TS-830S and TS-940S has
about the same bandwidth at minus 50db, but it has a much better
shape factor and it is mechanically and electrically interchangeable
with the stock filter in the TS-440S. The better filter is a muRata
CFJ455K12 or CFJ455V12, which will noticeably improve the transmit
and receive, SSB audio quality of the TS-440S. This filter is
available from Trio-Kenwood as p/n: L72-0333-05 for $42.89 {Dec
1989}. If you want SSB double-filtering in the 440's RX, the TS-940S'
matching, 8.83MHz, YK-88-S1, 2.7kHz SSB filter is available from
Trio-Kenwood as p/n L71-0222-05]. for $66.62 {Dec 1989}. This filter
goes in the optional SSB filter space on the IF Unit. For listening
to an uncastrated-male voice, the YK-88-S1 will produce
better-sounding, and more understandable, audio than the
Kenwood-recommended optional YK-88-S, 2.4kHz filter. A pair of TS-940
SSB filters will give the 440 the same superb selectivity that comes
with the 940.
Alignment: Supply a signal to the receiver. Set the TS-440S'
selectivity switch to M2, the single filter position. The USB and LSB
carrier oscillators [DIP switches on Control Unit] should be reset so
that there is roughly 20db of RX, SSB carrier-suppression for each
sideband at zerobeat. [use the 440's 20db ATTN as a standard] {Use
15db rolloff at zero-beat for more low-end audio, or 25db roll-off
for more high-end audio and/or better unwanted sideband suppression}
This completes the alignment of the carrier oscillators. >>>
If you installed BOTH filters: on LSB tune the 440 above the
calibrator's zerobeat frequency and note the 20db (or the roll-off db
you used above) roll-off point. This should be around 3.1KHz,
±200Hz higher than zerobeat. Put this frequency & LSB into
VFO B. Put the zerobeat frequency & LSB into VFO A. With the
Selectivity switch set to M1 [double SSB filter], the 8.375MHz
oscillator on the IF Unit is adjusted [TC2, in the lower left corner
of the PC board] so that the improved skirt selectivity on the double
filter position is equally distributed between the zerobeat 20db
rolloff point [VFO A] and the high-frequency 20db rolloff point [VFO
B]. The comparison can be done by watching the S meter and repeatedly
pushing the A/B button on the 440. [use fast AGC to reduce settling
time] Note 1: TC2 is installed backwards on the PC board so that the
rotor adjustment slot on TC2 is hot instead of grounded. This causes
the capacitance of TC2 to change when a metal screwdriver is used to
make the adjustment. To fix this problem, TC2 is removed, reversed
180 degrees and re-soldered on the PC board. Note 2: see IF Unit
schematic, CF2, the AM filter. There is a 1K Ohm resistor [R49] in
series with the input [D13] to the filter. This resistor provides a
closer impedance match between the 2000 Ohm filter and the source
[L4]. A similar resistor can be installed in series with D12 at the
input to CF1.
PROBLEM: RX audio distortion. {This problem seems to be more
prevalent in early production radios. There may have been a recent
factory component change to reduce receive distortion.} There is one
designed-in source of distortion and several other possible sources
of distortion. The designed-in source of distortion exists because
not enough forward bias current is applied to the switch diodes that
select the SSB [D23] , AM [D24] , and FM [D25] audio detectors.
Here's why: A mixer is a nonlinear device. Nonlinearity and
distortion go hand in hand. Diodes make good mixers when their
forward current is in the range of 0.05mA to about 0.6mA. At currents
above 1.5mA, diodes are reasonably linear and they make good
switches. The switch diodes in the TS-440S have enabling currents of
from 0.2mA for FM to 0.28mA for SSB, so the switch diodes are
operating in the region of maximum nonlinearity, which results in
distortion. The fix is simple: Increase the forward bias DC-current
through the diodes to roughly 2mA. This is accomplished by decreasing
the resistance of each DC-bias resistor to about 1k Ohm. When these
resistors are decreased in value, the 5000 Ohm impedance of the
low-level audio circuits decreases to about 500 Ohms and the values
of the coupling capacitors must be increased accordingly to prevent a
rolloff of the low frequencies. Similarly, the resistors that are in
series with the audio signals in these circuits must be decreased in
value to offset signal attenuation. The capacitance of the filter
capacitors between switch diode bias resistors (for SSB: C52,
4.7µF) must be increased to compensate for the decreased value
of the bias resistors.
"FIX for SSB audio detector and D23 switch: In the left, rear corner
of the IF Unit, change: R71, R73, R74, and R85 to 1k Ohm; C53 to
47µF, 10V [Xc=68 Ohms at 50Hz]; C52 to 22µF, 16V.
I'm guessing that similar changes can be made in the AM and FM
detectors. This project can become tricky since some of the needed
changes can also affect the transmit÷receive transition
performance of the radio. Thus, it may be necessary to compromise by
lowering the switch diode bias current to about 1mA. In general, this
can be done by using 2k Ohm, instead of 1k Ohm, bias resistors.
If, after the changes are incorporated, you can still hear RX
distortion on SSB, the problem may lie at the
[right-adjacent} product detector. Possible FIX: Install the missing
injection-oscillator terminating-resistor at the product detector.
This resistor is 62 Ohm, 1/8W or 1/4W. It is soldered under the IF
Unit PC board, near L5. The terminating-resistor is soldered to the
junction of R69 and R70 and the ground foil at the edge of the PC
board. If the distortion persists, you may have an unmatched set of
Germanium product-detector diodes: D19, D20, D21, and D22. These
diodes can be replaced with Schottky diodes. The product detector
balance should then be checked and adjusted as follows: Connect an RF
detector to the emitter of Q9/R77. R77 sticks up from the board at
one end so that the test connection can be easily made. The RF
detector can be an oscilloscope, detector/probe for a DMM, or a
455KHz receiver coupled through a 10pF capacitor. With no signal
input to the ANT jack, turn the RF Gain on the 440 to zero. Set mode
to USB, IF Shift to detent. Adjust TC1 [also installed backwards,
like TC2] for minimum RF. End of test. Reset the RF Gain control to
normal.
PROBLEM: AGC overshoot while receiving strong SSB signals. The
symptom is audio distortion on peaks only. The distortion is reduced
when the RF-gain control is backed off. FIX: On the RF Unit, near
J13, near Q5, change R42 from 470k Ohm to 10k Ohm. This speeds up the
attack response of the AGC.
PROBLEM: TX frequency response is not the same as RX frequency
response with the IF Shift control set on detent. FIX: Connect a
frequency counter to IF Unit, J26, pin 2 and ground. With the IF
Shift on detent, the frequency [roughly 455kHz] of the carrier
oscillator should not change between TX and RX. If the frequency
changes, adjust VR7 until the frequencies are equal. VR7 is just
behind the MIC pot and the top of the front panel; it is mounted on a
small, PC board.
INTERMITTENTS. The interconnecting wires in the TS-440S are copper.
The tin-plated single-row connector pins that are crimped to these
copper wires form a dissimilar metal junction that is subject to
electrolytic action due to moisture in the air. Some of these crimp
connections may eventually fail to provide electrical contact due to
electrolysis. FIX: Remove the defective connector pin by depressing
the ratchet-tab in the slot on the side of the connector pin and
pulling the freed pin from the connector body. [The ratchet-tab can
be depressed with a small screwdriver.] The copper wire that
protrudes past the crimp is then electrically bonded to the pin with
solder or Silver Print [GC Electronics] conductive paint. The
wire/crimp junction should be inspected with a magnifier before the
pin is re-inserted into the connector. If a wire/crimp junction is
soldered instead of being dabbed with conductive paint, it is
difficult to prevent the heat from melting the plastic insulation on
the wire. If soldering is the choice, the rosin flux residue should
be removed from the pin with alcohol, or acetone.
The same type of intermittent problem may also occur in the coaxial
connectors. The fix is to apply conductive paint between the crimp on
the center conductor pin and the copper wire.
An intermittent frequency display or wandering SSB receive frequency
can be caused by a dirty socket-to-chip contact on IC52 in the
Control Unit. On later production radios, IC52 may be soldered in.
The same symptoms can also be caused by a bad solder connection on
R152 in the 36MHz VCO [VCO #5] at the front-center of the PLL Unit,
near T20. Another common problem with VCO5 is L41 [10µH] which
apparently suffers from an intermittent internal connection. L41 is
potted, so the best fix may be to replace it.
A very common problem with VCO5 is that the type of glue that
is used to mechanically bond the components together appears to
absorb moisture from the air (it is hygroscopic). Since water has a
dielectric constant of 79, its presence can cause much grief in an RF
circuit. Thus, the moisture that is absorbed into the glue can cause
the oscillator to unlock. FIX: Remove the original glue with solvent
and a knife. If the glue is not replaced, VCO5 will exhibit
microphonic problems. Some types of clear hot-glue seem to work well
for replacing the original glue. Re-adjust VCO5 after the glue has
set up.
PROBLEM: No direct access to RX input or RX mute. These capabilities
are necessary if the 440 is to be used as a slave-receiver in
conjunction with another transceiver. FIX: On the IF Unit, connect a
wire from the base of Q39 to J22, pin 2. Remove R176, near J22. On
the X41-1610-00, (M/14) Switch Unit at the rear of the 440, jumper
across R46 [10K Ohm]. The RX will now mute when the FSK IN jack is
grounded. {FSK TX is still possible if the AFSK is fed into the MIC
jack through a 10 to 1 voltage divider.} The receiver input access
can be brought out to the ACC 3 connector by connecting a 27 Ohm to
51 Ohm 1/4W resistor to J29, pin 2 on the X41-1610-00, (N/14 ) Switch
Unit. A short length of wire connects the other end of the 1/4W
resistor to the center of the ACC 3 jack which is now the RX input.
When slaved to another transceiver through the transverter port, this
arrangement allows the operator to simultaneously listen on 2
frequencies with stereo earphones. This provides an advantage to the
user when working DX on split frequencies.
PROBLEM: There is no way to adjust the reference frequency oscillator
with the case on. If the frequency is adjusted with the case off, the
frequency will be different with the case on. FIX: drill a 7mm to 8mm
hole in the left side of the bottom half of the case. The hole should
line up with TC1 on the PLL Unit. The position of the hole can be
located with the case in place. The horizontal measurement is 122mm
back from the edge of the front panel that wraps around the left side
of the radio. The vertical measurement is 6mm below the edge of the
top half of the case that overlaps the bottom half of the case.
To adjust TC1: [You must have 10Hz readout enabled] Tune to 10.00000
MHz WWV, USB or LSB. Select W [wide] on the selectivity switch. Wait
until the tone modulation is present. You will hear both sidebands.
If the 2 tones are not the same, adjust TC1 until the tones
zerobeat.
PROBLEM: On QSK and on SSB VOX, it does no good to back off the RF
Gain control to reduce the nuisance of static crashes or band noise.
This is because the factory stock receiver comes on full-bore
whenever the TS-440S transitions from TX to RX - even if the RF Gain
is backed off! FIX: On the IF Unit, change R36, near Q5, to 2M Ohm;
change R60, near Q7, to 510K Ohm. ± a few standard values will
make little difference.
PROBLEM: Your own transmit RF gets into the TS-440S through the EXT
SP jack and causes audio rectification that is heard in the external
speaker. FIX: The sleeve/shield terminal on the EXT SP jack should be
bypassed to ground on the (G/14) Switch Unit with a 2nF to 20nF,
500V, disc ceramic capacitor. If the problem is most severe on 10
meters, try 2nF [.002µF]. If the trouble is most severe on 80m
or 40m, try 20nF [.02µF].
PROBLEM: You can hear distorted audio coming out of the internal
speaker while you are transmitting on SSB. FIX: Remove the top cover
on the radio and re-position the internal speaker wires away from the
area around the SSB filters. The speaker wires should be confined to
the area around the speaker plug on the IF Unit. Also, keep the
speaker wires away from the Control Unit behind the digital
display.
PROBLEM: Key-clicks on CW. This is caused by too fast (500µS) RF
output rise [make] and fall [break] times. FIX: On the IF Unit,
change C168, near Q49, to .22µF; change R225 to 33K Ohm-43K Ohm.
{the factory's "fix" for this problem is OK on make but it still
clicks on break}. Unfortunately, fixing the key-click problem also
seems to affect the full breakin make timing in the 440 which clips
the first dit. Thus, if you want to use the 440 on full, instead of
semi, breakin, you must put up with the key-clicks.
PROBLEM: The amplifier-keying-relay, RY2 on the (N/14) Switch Unit,
makes too much noise, or the contacts on RY2 have burned and pitted,
or all of the above. Another problem with RY2 is that it is too slow
to use with a full-QSK amplifier. This needless make-delay can cause
the amplifier to hot-switch, burning the contacts in its QSK-relays.
FIX: replace RY2 with an NPN switching transistor and fix the current
pulse problem that pitted the relay contacts, which may also damage
the transistor. [only works for amplifiers with positive voltage
relay control]. If your amplifier uses positive 110V for the relay
control, like the SB-220 and the TL-922, the relay pitting is caused
by the current pulse from the repeated shorting out of the charged
.02µF bypass capacitor across the amplifier's relay control
jack. The bypass-capacitor can be removed if shielded wire is used
for the interconnection cable to the transceiver. Another fix is to
install a 150 Ohm to 200 Ohm, 1/4W series resistor at the relay
control jack to limit the discharge current to a value that the relay
or switching transistor can handle. The bypass capacitor is connected
to the relay-side of the resistor.
Transistor Installation Notes: The N/14 Switch Unit is located
just behind the ANT RF connector on the rear panel. The small access
panel on the bottom, rear of the radio is removed to gain access to
the N/14 Switch Unit. Two chassis-ground connections and one center
pin connection must be unsoldered from the RF connector before the
Switch Unit can be removed. Unplug the three connectors, remove the
two sheet metal screws, and lift out the Switch Unit. Unsolder and
remove RY2, D16, and the white jumper-wire and the pin that it plugs
into. Install one 1k Ohm resistor each in place of D16 and in place
of the jumper-wire and its pin. The transistor will solder in place
of the relay if its full length leads are bent to fit the available
holes. The emitter goes to common-ground, as does the trace to J30,
pin4 [CMC], the ground return for the relay control circuit. The base
lead connects to the trace that goes to R2 {D16} and C37. The
collector solders to the trace that connects to J30, pin 2 [TXC].
PROBLEM: Poor skirt selectivity on AM. FIX: The unsatisfactory,
stock, TS-440S AM filter, CF2, can be directly replaced with the
better performing, AM-narrow, 6KHz filter from the Trio-Kenwood
R-1000 receiver. The part number of this filter is L72-0319-05 and
the price is $9.10 {Dec 1989}. It is available as a replacement part.
Even though the better filter has more pin connections and is
physically larger than the original filter, the IF Unit printed
circuit board was designed to accept either AM filter. The design
engineers must have realized that some people would want to install a
good AM filter.
CF2 is a small, black, cube-shaped plastic component at the rear of
the IF Unit just slightly to the right of left-to-right circuit board
center. No realignment is necessary after the AM filter is
replaced.
MAINTENANCE: The VFO tuning knob should be removed, after loosening
the 1.5mm hex-socket set-screw, and the tuning shaft's
bushing-bearing should be lubricated with a modern semi-synthetic
lubricant like Break Free or Tri Flow. The quantity of lubricant used
should be small and the radio should be tipped back to help the
lubricant run down into the bushing-bearing. This should be done once
when the radio is new and roughly every 4-years thereafter.
DOUBLE-SIDEBAND MODIFICATION FOR THE TS-440S
Occasionally, it may become advantageous to use
double-sideband-transmit and single-sideband receive mode in order to
thwart the efforts of radio sociopaths who are gratified by
interfering with others. DSB-xmit/SSB-RX mode gives the
non-interfering stations the option of listening to the sideband that
has the least amount of interference.
To install DSB capability in the TS-440S, the audio processor switch
is rewired so that when the switch is depressed, the carrier is
removed from the AM transmit signal. Without a carrier, AM becomes
DSB. {The DSB modification will disable the less-than-worthless
audio-PROCessor in the TS-440S.}
The modification: On the IF Unit [the top board] locate R179, which
is between IC4 and Connector 21 at the front, left of the circuit
board. Remove R179 and connect a jumper wire from the right hand,
empty solder-pad hole on the circuit board [collector of Q41] to the
junction of D45 and R196, which is straight back on the circuit
board, just to the left of IC5; about 4cm from the rear of the
circuit board.
To enable DSB transmit/SSB receive, "SPLIT" operation is
utilized:
1. Program VFO A=B.
2. Program VFO A for either USB or LSB, depending on which one has
the least interference.
3. Program VFO B for AM and push the PROC [DSB] switch in to remove
the AM carrier.
4. Select VFO A.
5. Program SPLIT operation. The 440 will now listen on VFO A and
transmit on VFO B.
6. Set the carrier control straight up to position #5 [12
o'clock].
7. While transmitting, adjust the MIC gain control for a small amount
of ALC. This keeps the DSB bandwidth to a minimum.
While listening [VFO A], it may be necessary to select the sideband
that has the least amount of interference. If your friends are also
transmitting on DSB, you may be able to continue communicating,
despite the efforts of those who would like to spoil the enjoyment of
others.
>>>DSB should not be used unless the other sideband is
vacant. If the interfering station or stations can cause the
group that they are interfering with to interfere with a third group,
it will definitely make their day.
Most jammers enjoy being talked about, either positively of
negatively. This is why they usually switch back and forth between
receive and transmit. If you want a jammer to stick around, talk
about him. Stupid insults usually work best.
End